Page 75 - KBHA BULLETIN 5
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               The  trawler  ran  aground  opposite  Kalk  Bay  Station  and  succumbed  to  the  sea  within  a  few

               months.  (Fig.  4.7.)  Her  boiler,  however,  which  was  washed  up  alongside  the  railway  station,

               remained there for many years and could be seen on postcards of Kalk Bay as late as 1910. The
               244-ton trawler, which was newly bought by the False Bay Fish and Cold Storage Company, had

               sailed from  England on  her maiden voyage. She was  loading ice at  Kalk  Bay  when  a strong
               south-easter caught her captain unawares. She dragged anchor and was soon aground. Her ten-

               man crew reached the shore safely, but  she was a total  wreck. A salvage auction held  on 28

               October realized only £51-12-6, which included the trawl nets and coal. Her master was blamed
               for bad seamanship, although the equipment was said to be faulty. This did not help with any

               insurance claims and resulted in the financial demise of her owners.



               The following report in the Sea Side News of 24 October 1903, with the final punch-up at the
               Kings Hotel, makes interesting reading.



                       Steam trawler REX, 244 tons, was bought in England and brought to South Africa by the
                                                                                                  rd
               False Bay Fishing and Cold Storage Co. Ltd. She sailed from Simon’s Town 7.a.m. 3  Oct 1903.
               At 10.30 she anchored off Kalk Bay to collect ice from the cold storage. While waiting for the
               second load of ice to be brought out she started to drag anchor under the influence of a south-east
               wind. Although the vessel had ‘steam up’ she drifted onto the rocks between 1300 and 1400,
               close to the railway station. Telegrams were sent immediately to Simon’s Town and within an
               hour  the  powerful  tug  of  the  Admiralty  Scotchman  and  steam  trawler  Marie,  another  of  the
               company’s steam trawlers, attempted to tow Rex off the rocks. Unfortunately she had sprung a
               leak and was taking water, and it was decided to leave her where she was until the extent of the
               damage was known. When the stranding occurred 10 men were on board, but they managed to
                                                                                                        st
               get ashore without difficulty. The Captain was David C. Newbury. She also had a mate, a 1  and
                 nd
                                                                    th
               2  Engineer and a cook. The Court of Enquiry on 20  Oct 1903 found the Rex had anchored in
               an  unsafe  position,  a  proper  and  good  watch  had  not  been  kept,  the  anchors  and  associated
               equipment were defective and inefficiently used, and previous to the time of stranding the vessel
               was navigated in a careless, unseamanlike manner and the whole discipline of the ship appeared
               to have been bad. The Master was accordingly held responsible and his certificate suspended for
               3 months.









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